1987 26 ft LS Scarab....$?
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Location: Mooresville, NC
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Cornelius, NC in a storage lot. I had been watching it for a long time but every time I drove by was after hours. One day in November I found myself driving by early enough that the office was open. I stopped in and told the lady inside I was interested in it and asked her to give my name and number to the owner. She called him while I was there and left a message. He called me the next day and we put a deal together. He gave me the pass code to get in the gate and I checked it out that weekend. That's when I took the "before" pictures I originally posted.
Last edited by Hondo Jet; 07-26-2010 at 05:48 PM.
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looks great ! If you ever have to paint it, loosing them bow rails would look super clean!! I think I like that better than the rounded windshield CV's that came after !!!!!
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Here are some more pictures.....
I have not done anything with the interior yet, but I found a really nice set of Imco Powerflows that I put on it.
The last time I had it out every it ran great until I hit 4000 rpm it would start popping and running terrible. I figured it had to be ignition so I put a MSD Pro Billet distributor and a 6A that I had in the garage. Yes, the black wire is off of the coil because i took this picture after I unpluged it when the box started smoking.
This 6A is one that bit the dust before and I sent it back to MSD for repair. They charged me $75 plus freight and sent it back and said it was good as new. It ran great for about 5 minutes then bit it again. How can you possibly go wrong with a hot, a ground, ignition and coil wires. Well so much for my $75. Fortunately this nice family was close by and towed me back to my trailer.
The last time I had it out every it ran great until I hit 4000 rpm it would start popping and running terrible. I figured it had to be ignition so I put a MSD Pro Billet distributor and a 6A that I had in the garage. Yes, the black wire is off of the coil because i took this picture after I unpluged it when the box started smoking.
This 6A is one that bit the dust before and I sent it back to MSD for repair. They charged me $75 plus freight and sent it back and said it was good as new. It ran great for about 5 minutes then bit it again. How can you possibly go wrong with a hot, a ground, ignition and coil wires. Well so much for my $75. Fortunately this nice family was close by and towed me back to my trailer.
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I got it out the other weekend and took it to the water. Started up and idled fine until it started sucking water out of the fuel tank. Apparently the fuel fill o-ring is compromised and over the winter water was gettting past it into the tank. I drained the tank and cleaned out as best as I could, had to flush the water out of the carb bowls and all seemed to be fine. I have had a lot of problems with my 9022 carb transitioning from idle to primary circuits without pumping the throttle. Then I have to ease in to it slow to keep it from popping back through the carb. This weekend I got fed up enough that I pulled of the 780 Vacuum secondary carb off my '66 Chevelle and put it on the boat. It worked flawlessly from the second I fired it up to wide open. Never missed a beat and ran about 2 mph faster than the last time I had it out.
Last edited by Hondo Jet; 06-06-2011 at 09:33 PM.